廖秋林, 李腾飞, 李润军, 孙宏宝, 谭文辉. 2016: 暗挖隧道杂填土地层马头门支护与开挖方法分析. 工程地质学报, 24(4): 668-673. DOI: 10.13544/j.cnki.jeg.2016.04.024
    引用本文: 廖秋林, 李腾飞, 李润军, 孙宏宝, 谭文辉. 2016: 暗挖隧道杂填土地层马头门支护与开挖方法分析. 工程地质学报, 24(4): 668-673. DOI: 10.13544/j.cnki.jeg.2016.04.024
    LIAO Qiulin, LI Tengfei, LI Runjun, SUN Hongbao, TAN Wenhui. 2016: STUDY ON SUPPORT AND EXCAVATION OF HORSEHEAD IN THE RESERVED SHAFT OF A TUNNELL. JOURNAL OF ENGINEERING GEOLOGY, 24(4): 668-673. DOI: 10.13544/j.cnki.jeg.2016.04.024
    Citation: LIAO Qiulin, LI Tengfei, LI Runjun, SUN Hongbao, TAN Wenhui. 2016: STUDY ON SUPPORT AND EXCAVATION OF HORSEHEAD IN THE RESERVED SHAFT OF A TUNNELL. JOURNAL OF ENGINEERING GEOLOGY, 24(4): 668-673. DOI: 10.13544/j.cnki.jeg.2016.04.024

    暗挖隧道杂填土地层马头门支护与开挖方法分析

    STUDY ON SUPPORT AND EXCAVATION OF HORSEHEAD IN THE RESERVED SHAFT OF A TUNNELL

    • 摘要: 城市隧道暗挖施工期间拱顶以及地表的沉降量对施工安全、工程功能及城市道路正常运行具有重要意义。浅埋暗挖法施工中各类马头门的施工因其受力转换特殊往往是施工过程中关注的重点。北京地铁7号线某区间暗挖隧道马头门处于竖井明挖施工的回填土中,其土质情况复杂、暗挖不确定性因素多。为保证隧道施工和周围构筑物的安全,须对处于回填土范围内竖井马头门的破除与开挖方案进行研究。本文根据地表勘察钻探和超前探测所获取的地层资料和工程设计资料,应用FLAC3D软件对马头门破除时的两个支护方案进行了对比分析。施工实践与理论分析均表明,采用无收缩(WSS)深孔注浆方案的地表沉降量约是超前小导管支护方案沉降量的1/2~1/3。

       

      Abstract: During tunneling construction in subways, the settlement in arch crown and ground will greatly impact on the construction safety, engineering function and normal operation of urban roads. The soil around the reserved shaft in Beiwan region of No.1 section, No.7 Subway of Beijing is backfilled and complex. In order to ensure the safety of tunneling construction and structures, it's necessary to do schematic studies on the removal and excavation of horsehead in backfill soils. Based on the data of surface survey drilling and prediction detection of the strata and the engineering design data, the software FLAC3D is used to study the two reinforcement schematics when the horsehead of the reserved shaft is exploded, also, the arch crown and ground settlements resulted from the construction of six pilot tunnels in the rectangular transient cross-section are simulated and compared with the monitoring results of pilot tunnels' excavation. The research showed that when the horsehead is removed, the settlement using non-shrinkage grouting of deep hole method was one third to a half of that using advanced small pipe support method.

       

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