刘满林, 刘升传, 丁桂伶, 王连俊. 2007: 既有线重载铁路路桥过渡段路基基床病害及整治措施研究. 工程地质学报, 15(S1): 576-583.
    引用本文: 刘满林, 刘升传, 丁桂伶, 王连俊. 2007: 既有线重载铁路路桥过渡段路基基床病害及整治措施研究. 工程地质学报, 15(S1): 576-583.
    LIU Manlin, LIU Shengchuan, DING Guiling, WANG Lianjun. 2007: RESEARCH ON BED DEFECTS IN RAILWAY-BRIDGE ABUTMENT SUBGRADE AND THEIR TREATMENT IN EXISTING HEAVY-LOAD RAILWAY LINE. JOURNAL OF ENGINEERING GEOLOGY, 15(S1): 576-583.
    Citation: LIU Manlin, LIU Shengchuan, DING Guiling, WANG Lianjun. 2007: RESEARCH ON BED DEFECTS IN RAILWAY-BRIDGE ABUTMENT SUBGRADE AND THEIR TREATMENT IN EXISTING HEAVY-LOAD RAILWAY LINE. JOURNAL OF ENGINEERING GEOLOGY, 15(S1): 576-583.

    既有线重载铁路路桥过渡段路基基床病害及整治措施研究

    RESEARCH ON BED DEFECTS IN RAILWAY-BRIDGE ABUTMENT SUBGRADE AND THEIR TREATMENT IN EXISTING HEAVY-LOAD RAILWAY LINE

    • 摘要: 重载铁路路桥过渡段由于刚性桥台结构物和柔性路堤连接处所产生的刚度差,以及在桥台台尾连接地段因重载列车行车荷载的反复作用,使得静态不平顺、动态不平顺同时存在的条件下,填土在固结沉降过程中易产生较大的差异沉降。这一现象将随着车速的提高和轴重的增大而加剧。因此,对重载铁路过渡段轨下基础的研究具有异常重要的意义。发展重载铁路,路基压实质量的好坏直接影响运输的安全和效能,但长期在"重桥隧轻线路,重线路轻路基"的偏向下,路基填料选用要求低,压实标准低,检测频率少,致使既有线运营铁路路基技术状态不佳,产生路基基床病害,已成为铁路运输的主要薄弱环节,严重威胁铁路运输安全。本文综述了前人所作的工作内容,并借鉴了相关的研究方法,指出既有线路基基床病害的产生原因及机理,并介绍了目前采用的处理措施。对朔黄铁路第170号桥(K361+904)以及桥梁两端路桥过渡段路基进行了现场测试,包括地质雷达检测、和路基整体调查等;通过测试结果分析了该过渡段路基基床的压实质量及存在的问题,针对问题提出了相应的加固处理措施,采用倾斜桩和水平桩进行处理,并用有限元软件对其加固效果进行了模拟。

       

      Abstract: For railway-bridge abutment, the fill soil is easy to produce large different settlement in the course of consolidation settlement when the static state and dynamic state irregularity are all concurrent. It is because there is a stiffness difference in the linking part of abutment structure and soft embankment and the repeating action of train loading in abutment trail. This phenomena will become serious with the increasing of train's velocity and axle load. Therefore, it is very important to study the foundation under rail of high speed railway abutment. On the other hand, Subgrade compaction quality has a direct influence on the heavy load railway and its transportation safety. Because the need of the fill soil using in subgrade and the compaction standard is low as well as the checking frequency is little, the existing railway line subgrade technique and state is bad which has become the main weak aspect of the railway and threaten the safety of transportation. And the work which have been done is introduced in this paper and is used for reference of the methods. Firstly, based on the railway ministry project-existing railway line railway-bridge abutment subgrade and rail strengthen research, we have tested Shuo-Huang railway 170th bridge and railway-bridge abutment subgrade in field. The testing projects include geology seismic test. The results reflect the subgrade quality and problems behind this abutment. Then the countermeasures are brought forward to strengthen the subgrade aspects which need deal with. The plane piles and slanting piles are used associatively has a more obvious effect. The strengthening impact is also simulated by FE procedure and the results are satisfied.

       

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